ij39
Petroleum
- Nov 23, 2010
- 3
a 72 hour pressure build-up test was run on a unconventional tight gas/liquids formation
horizontal tvd 12,132'
rih gradient rih - both pressure/temperature stair stepped all the way in then stabilized
pooh gradient pooh - both pressure/temperature stair stepped all the way out
this may not be enough information for help - might be a start
is it possible that some of the balls have not released and that pressure/temperature flucuations occurring go away when the balls reseat - if that is the case we will have to go in with coiled tubing unit - we also feel there may be some formation material in the lateral that is effefecting the production - the well has not performed as expected
thanks
IJ
horizontal tvd 12,132'
rih gradient rih - both pressure/temperature stair stepped all the way in then stabilized
pooh gradient pooh - both pressure/temperature stair stepped all the way out
this may not be enough information for help - might be a start
is it possible that some of the balls have not released and that pressure/temperature flucuations occurring go away when the balls reseat - if that is the case we will have to go in with coiled tubing unit - we also feel there may be some formation material in the lateral that is effefecting the production - the well has not performed as expected
thanks
IJ