npower0073
Electrical
- Jun 24, 2007
- 70
Dear all. On site we have a 9FA DLN +2 gas turbin coupled with a hydogen cooled 270MW generator. After the end of a combustion inspection outage we saw the following : When GT goes from 140 MW to base load 260MW then we see increase readings on the proximity of bearing 1 (TE) of generator. When the load decreases we saw decrease of the rpoximity reading. THe seismic sensors have increase as well but far below limits. We suspect possible air leaks from turbine that lead to possible thermal expansion of turbine and change of mechanical load of the generator. Let me know your opinion. Nothing has changed as far it concerns hydrogen purity, bearing metal and oil temperatures, ambient air etc.